SPE Asia Pacific Oil and Gas Conference and Exhibition 2012
DOI: 10.2118/159108-ms
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When Control Line Fails, What is the Alternative?: West Malaysia Experience

Abstract: Angsi X06L was a firm candidate for a workover targeted to be re-completed in April 2010. This well was diagnosed with a severe downhole control line leak, causing the well to be shut in and led to Angsi field deferment of 800 barrels oil per day. PETRONAS Carigali Sdn Bhd (PCSB) had already attempted to rectify this problem by injecting pressure activated sealant a few times but failed in its efforts. Based on the diagnostic done, the leak rate was more than 1.5L/min, way beyond the selected activated sealant… Show more

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