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Agbami Wells; Agbami A, Agbami B and Agbami C experienced significant production decline. A multi-disciplinary team from the Agbami Asset initiated a study to identify the cause of damage to the wells and the best mitigation strategy. The study confirmed fines migration as the primary cause of sandface impairment and recommended an acid formulation to cure the damage. Risk analysis was undertaken to ascertain the problems associated with flowing the acid back to the production facilities. An innovative deployment method involving a marine support vessel with dynamic positioning and Remote Operating Vehicle (ROV) was adopted. Utilizing the marine support vessel, a customized dual conduit of coil tubing was employed to bullhead acid into the formation. The acid was allowed to soak in the formation for a few hours and well opened to flow back naturally to surface. Other critical aspects of the job planning and implementation included ensuring pump rates were achieved, designing appropriate acid volumes and soak duration, proper planning of Site Integration Test (SIT) and coil tubing deployment strategy. Stimulating Agbami A, Agbami B and Agbami C led to a total incremental gain of 17,500 BOPD with a reduction in skin of over 70%. Productivity Index (PI) increased by over 50% on all the wells. Lessons Learned include: Dual coil string provides redundancy in the event of failure of one of the strings Identifying the cause of damage is critical in recommending acid stimulation for remedial work Adequate front end loading and proper stakeholder engagement was critical to ensure success This technical paper describes the steps involved in implementing a successful rigless acid stimulation operation on deep water wells offshore Nigeria and will be a key resource document for future acid stimulation wellwork.
Agbami Wells; Agbami A, Agbami B and Agbami C experienced significant production decline. A multi-disciplinary team from the Agbami Asset initiated a study to identify the cause of damage to the wells and the best mitigation strategy. The study confirmed fines migration as the primary cause of sandface impairment and recommended an acid formulation to cure the damage. Risk analysis was undertaken to ascertain the problems associated with flowing the acid back to the production facilities. An innovative deployment method involving a marine support vessel with dynamic positioning and Remote Operating Vehicle (ROV) was adopted. Utilizing the marine support vessel, a customized dual conduit of coil tubing was employed to bullhead acid into the formation. The acid was allowed to soak in the formation for a few hours and well opened to flow back naturally to surface. Other critical aspects of the job planning and implementation included ensuring pump rates were achieved, designing appropriate acid volumes and soak duration, proper planning of Site Integration Test (SIT) and coil tubing deployment strategy. Stimulating Agbami A, Agbami B and Agbami C led to a total incremental gain of 17,500 BOPD with a reduction in skin of over 70%. Productivity Index (PI) increased by over 50% on all the wells. Lessons Learned include: Dual coil string provides redundancy in the event of failure of one of the strings Identifying the cause of damage is critical in recommending acid stimulation for remedial work Adequate front end loading and proper stakeholder engagement was critical to ensure success This technical paper describes the steps involved in implementing a successful rigless acid stimulation operation on deep water wells offshore Nigeria and will be a key resource document for future acid stimulation wellwork.
This well was drilled and completed as a Frac & Pack oil producer with subsea wellhead in 3300 ft water depth. Despite all the care taken to maintain cleanliness during completion, initial performance on starting up the well indicated that it was severely impaired during the drilling phase with drawdown as much as 2300 psi observed. The well initially failed to reach the Hydrate Dissociation Temperature (HDT) of 35C within the specified period of 1 hour. The well was eventually successfully started and some performance improvement was observed as the well was cleaned up gradually over the next few months but the potential of the well had to be revised down from the planned 30kbpd to 12kbpd to honour drawdown limit of 350psi. This paper documents the effort made to restore the well's planned production of 30kbpd by acid stimulation treatment by bullheading from the rig. From the well history, the source of impairment was attributed to drilling fluids. Thus, a half-strength mud acid was chosen as the treatment fluid and the placement was by high-rate bullheading from the rig connected to the subsea Xmas tree via a riser and EDP/LRP. The risk of flowing unspent acid through subsea flowlines and topsides equipment on the FPSO was assessed. Corrosion simulation studies showed the subsea flowlines can withstand the possible unspent acid with proper dilution by flowing high water cut wells at high rate through the same bulk flowlines being used to unload the just treated well. The dilution also helped protect the topsides equipment while further protection was provided by injecting diluted sodium hydroxide into the flow stream as it enters the topsides. The result of the treatment was that productivity index increased by a factor of 3 from 27 bpd/psi to ca. 90 bpd/psi and the well is now producing at 30 kbopd.
As the global well base continues to increase, it is becoming apparent that under-investment in maintenance has helped contribute to a decreasing average production per subsea well. To combat this trend, more focused and cost-effective intervention techniques have emerged such as open-water hydraulic access (OWHA) using coiled tubing (CT). OWHA using CT provides operators with a fit-for-purpose solution to deliver fluids to a subsea well without the requirement for mechanical intervention. In scenarios which meet the requirements outlined within this paper, OWHA using CT offers an attractive alternative to conventional intervention approaches. Three predominant configurations of OWHA CT systems are apparent, all developed around differing drivers: a conventional system using a CT injector head (IH), a specialized system using a CT IH, and a powered reeler with deployment sheave. Both the benefits and limitations of each are considered to guide the reader in selecting the correct configuration for their application. The primary cost driver for hydraulic intervention is vessel selection. Factors including regional availability, mobilization requirements, and specification are key to the selection process. An advantage of OWHA using CT is the ability to use a vessel of opportunity due to the decreased equipment footprint and specification; this directly enhances service flexibility and cost management. When compared to alternative oil sources, the comparative cost per barrel of oil unlocked by OHWA is at least 43% less than the closest alternative. When compared to alternative intervention approaches, the simplified equipment and requirements result in a reduced total cost thus enhanced return on investment with accelerated payback. Using average global vessel rates and generalized assumptions, for a single well intervention the total costs can be in the order of the following magnitudes: floating rig USD 9-16M, light well USD 6-10M, OWHA USD 2-5M. Using an average well production gain of 1,950 BOPD this gives a typical payback time period of ~9 months for a rig and ~3 months for OWHA. In scenarios which meet the requirements outlined within this paper, OWHA provides the most economical solution with the ability to provide positive returns in the same financial year.
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