2018
DOI: 10.3390/aerospace5010031
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CFD Validation and Flow Control of RAE-M2129 S-Duct Diffuser Using CREATETM-AV Kestrel Simulation Tools

Abstract: Abstract:The flow physics modeling and validation of the Royal Aircraft Establishment (RAE) subsonic intake Model 2129 (M2129) are presented. This intake has an 18 inches long S duct with a 5.4 inches offset, an external and an internal lip, forward and rear extended ducts, and a center-positioned bullet before the outlet. Steady-state and unsteady experimental data are available for this duct. The measurements include engine face conditions (pressure recovery, static pressure to free-stream total pressure rat… Show more

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Cited by 10 publications
(5 citation statements)
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“…Aref et al [55] used the Q-criterion to explain the vortical structure formation in a RAE-M2129 air intake. A value of Q > 0= 0.1) is chosen in the present article to generate iso-surfaces for visualising the vortices generated by the synthetic jets during the blowing (Fig.…”
Section: Vorticity Dynamics and Q-criterionmentioning
confidence: 99%
“…Aref et al [55] used the Q-criterion to explain the vortical structure formation in a RAE-M2129 air intake. A value of Q > 0= 0.1) is chosen in the present article to generate iso-surfaces for visualising the vortices generated by the synthetic jets during the blowing (Fig.…”
Section: Vorticity Dynamics and Q-criterionmentioning
confidence: 99%
“…On the other hand, hybrid systems can have an additional benefit on performance parameters, compared to passive or active flow control alone [41]. As to mixing the mainstream and the secondary flow, some passive flow control technology, such as the vortex generator, shows great potential [42][43][44][45][46][47]. So, in this additional suction supplementary method research section, large mass flow suction control has been researched first, and then the combination of the micro-suction control and the vortex generator control.…”
Section: Additional Improvement For the Original Suction Controlmentioning
confidence: 99%
“…both orientation of object with respect to the axis of the intake duct at the entry and angle of attack for aircraft was varied and simulated. Studies have been performed on estimating the trajectory of a store separation 1 and for understanding the flow inside an S-type diffuser duct [4][5][6][7] .…”
Section: Validationmentioning
confidence: 99%
“…As explained earlier, the design of the duct and the presence of the bird cause non-uniformity in the flow. This could affect the surge margin and lead to stall 7 .…”
Section: Variation In Engine Face Pressure Recovery Pattern For Variomentioning
confidence: 99%