Day 2 Wed, October 30, 2019 2019
DOI: 10.4043/29741-ms
|View full text |Cite
|
Sign up to set email alerts
|

Effective Cross Flow Diagnostic by Pulse Neutron, Cement Logs and Fluid Production: Water Shut Off Well Case in Amo Field

Abstract: The high water cut 98,5% caused the abandonment of a directional well, which was reactivated after 3 years using a water shut off technique. Offset wells production behavior, stratigraphic seal layers distribution, reservoir properties, and cased hole logging data played a relevant role for the well planning, reactivation and production success of heavy oil from the mature Amo field in the Oriente Basin of Ecuador. The Lower U reservoir production screening from neighbor wells and stratigraphica… Show more

Help me understand this report

Search citation statements

Order By: Relevance

Paper Sections

Select...

Citation Types

0
0
0

Year Published

2020
2020
2020
2020

Publication Types

Select...
1

Relationship

0
1

Authors

Journals

citations
Cited by 1 publication
references
References 2 publications
0
0
0
Order By: Relevance