During the life firing test of 1 N-class thruster development model, pulse mode performance and performance changes were examined. The deviation of pulse mode response time according to thruster feed pressure was relatively small and the resultant ignition delay, response time, tail-off time were 32-35 ms, 86-91 ms, 89-98 ms, respectively. For the stabilized pulse region the impulse bit revealed the outstanding reproducibility of 1.41, 1.32, 2.10% at 3σ. During the life firing test, the impulse bit was decreased with limited amounts, therefore the pulse mode performance could be considered to be maintained. The thrust centroid was also maintained during the life firing test.