24th AIAA Aerodynamic Measurement Technology and Ground Testing Conference 2004
DOI: 10.2514/6.2004-2496
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Progress Report on the APTU Upgrade Activities

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Cited by 6 publications
(2 citation statements)
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“…(4) The scramjet fuel feed was cut off while vitiated air was supplied into the scramjet combustor. (5) The test terminated as the VAH gas supply valve closed. The room-temperature GN 2 was supplied for purge.…”
Section: Scramjet Combustor Preliminary Test: Forced Ignitionmentioning
confidence: 99%
See 1 more Smart Citation
“…(4) The scramjet fuel feed was cut off while vitiated air was supplied into the scramjet combustor. (5) The test terminated as the VAH gas supply valve closed. The room-temperature GN 2 was supplied for purge.…”
Section: Scramjet Combustor Preliminary Test: Forced Ignitionmentioning
confidence: 99%
“…Abundant experimental studies have used a blowdown-type facility. An aerodynamic and propulsion test unit (APTU) was constructed and tested by Garrard et al The APTU produced vitiated air using a butane and liquid oxygen sudden-expansion burner and provided a Mach number of 4.5, a total pressure of 2.07 MPa, a total temperature of 1111 K, and 12 min of test duration [5]. Meng et al constructed a variable Mach number direct-connected supersonic combustor test facility using a heater.…”
Section: Introductionmentioning
confidence: 99%