2021
DOI: 10.1016/j.istruc.2021.09.104
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Test on shear behavior of less-tightened high-strength bolted connections

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Cited by 4 publications
(1 citation statement)
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“…The peak load was reached at about 33.0 kN at 13.1 mm; then, a decrease of resistance occurred, accompanied with the slippage or breakage of some wires and damaging of mortar. By analyzing the envelope curves, an increase in stiffness emerges in the branch 2-5 mm, compared with the previous one, as already noticed by Sisti et al (2019), but this occurrence is realistically related to the shear behavior of the tightened bolts at the base connection (Lin et al 2021).…”
Section: In-plane Shear Testssupporting
confidence: 70%
“…The peak load was reached at about 33.0 kN at 13.1 mm; then, a decrease of resistance occurred, accompanied with the slippage or breakage of some wires and damaging of mortar. By analyzing the envelope curves, an increase in stiffness emerges in the branch 2-5 mm, compared with the previous one, as already noticed by Sisti et al (2019), but this occurrence is realistically related to the shear behavior of the tightened bolts at the base connection (Lin et al 2021).…”
Section: In-plane Shear Testssupporting
confidence: 70%