The cemented phosphogypsum (PG) backfill technique provides a new method for massive consumption of PG, and therefore alleviating the environmental pollution of PG. This study considered the effects of slurry preparation on the performance of cemented PG backfill. A L 16 (4 4 ) orthogonal experiment was designed to analyze four factors, namely the solid content, phosphogypsum-to-binder ratio (PG/B ratio), stirring time and stirring speed, with each factor having four levels. According to the range analysis, the solid content played the dominant role in controlling the bleeding rate, while the setting times strongly depended on the PG/B ratio. In terms of strength development of the backfill, the PG/B ratio was shown to be the most significant factor determining the unconfined compressive strength (UCS), followed by the solid content, stirring time and stirring speed. Furthermore, the results showed that the slurry preparation affected the environmental behavior of impurities that originated in PG. By analyzing the concentrations of impurities in the bleeding water of the slurry as well as the leachates of the tank leaching test, the results showed that the release of F − and SO 4 2− was aggravated clearly with the increase in the PG/B ratio, while the release of PO 4 3− always remained at relatively low levels.
In this study, the durability of phosphogypsum (PG)-based cemented backfill was investigated by drying-wetting cycles to explore deterioration of its strength and the release of impurities. The leachates in this test were composed of deionized water, 5% Na2SO4 solution, 5% NaCl solution, and a range of sulfuric acid solutions with pH values of 1.5, 3, and 5. After drying-wetting cycles, unconfined compressive strength (UCS), visual deterioration, porosity, microstructure and concentrations of phosphate and fluoride in the leachates were measured. The results showed that both saline and acidic solutions could lead to strength reduction of PG-based cemented backfill under different deterioration mechanisms. The mechanical damage of salinity was caused by micro-cracking and degradation of C–S–H. However, the H+ broke the backfill by dissolving hydration products, leaving the conjunctures between PG particles weakened. Furthermore, the environmental impact was investigated by measuring the concentration of phosphate and fluoride in the leachates. In acidic solutions, the release of phosphate and fluoride was greatly enhanced by H+. Compared to the great strength deterioration in saline leachates, the concentration of phosphate and fluoride were similar to that of deionized water, indicating that saline solutions had little impact on the release of hazardous impurities.
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