The use of separated overfire air (SOFA) has become a standard technique of air staging for NOx reduction in the coal-fired boiler and can also be applied to existing boilers by retrofit. This study was to optimize the air distribution for the proposed SOFA installation in a 500 MWe tangential-firing boiler that has 20 identical units in Korea. Using computational fluid dynamics (CFD) incorporating advanced coal combustion submodels, the reference case was established in good agreement with the design data, and different flow ratios of burner secondary air, close-coupled OFA (CCOFA), and SOFA were evaluated. Increasing the total OFA ratio effectively suppressed NO formation within the burner zone but had a negative impact on the boiler performance. With moderate air staging, NO reduction became active between the CCOFA and SOFA levels and, therefore, the OFA distribution could be optimized for the overall boiler performance. For total OFA ratios of 25% and 30% with respective burner zone stoichiometric ratios of 0.847 and 0.791, increasing the SOFA ratio to 15% and 20%, respectively, was ideal for decreasing the unburned carbon release and ash slagging as well as NO emission. Too high or low SOFA ratios rapidly increased the unburned carbon because of inefficient mixing between the strong air jets and char particles. Based on these ideal cases, the actual air distribution can be adjusted depending on the coal properties such as the ash slagging propensity.
For renewable electricity production, biomass can fully displace coal in an existing power plant with some equipment modifications. Recently, a 125 MWe power plant burning mainly anthracite in Korea was retrofitted for dedicated wood pellet combustion with a change of boiler configuration from arch firing to wall firing. However, this boiler suffers from operational problems caused by high unburned carbon (UBC) contents in the bottom ash. This study comprises an investigation of some methods to reduce the UBC release while achieving lower NOx emissions. The computational fluid dynamics approach was established and validated for typical operating data. Subsequently, it was applied to elucidate the particle combustion and flow characteristics leading to the high UBC content and to evaluate the operating variables for improving the boiler performance. It was found that the high UBC content in the bottom ash was a combined effect of the poor fuel grindability and low gas velocity in the wide burner zone originating from the arch-firing boiler. This prevented the operation with deeper air staging for lower NOx emissions. Reducing the particle size to <1.5 mm by modifying mills or pretreating the fuel using torrefaction was the only effective way of lowering the UBC and NOx emissions with deeper air staging while increasing the boiler efficiency.
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