Rice quaker are traditional food from the Sambas regency. The manufacture of rice quaker has been traditionally done by pounding it. Economically, the production capacity of traditionally made rice quaker is so low that it needs to be increased by changing the manual to mechanical flattening system. The purpose of this research is designing a prototype machine for flattening rice quaker as well as conducting experimental studies on the flattening process. The research stages were to design, manufacture, and test the performance of the flattening rice quaker. The independent variables of the study were the gap width and the number of flattening, while the dependent variables of the study were thickness and percentage damage of rice quaker. The width of the gap was varied into 0.4 mm, 0.6 mm, 0.8 mm, and 1.0 mm, while the number of flattening was varied to 1, 2, and 3 times the flattening. The result of the construction of the prototype rice quaker machine is in accordance with the initial design, and can work to flatten rice quaker. The engine test was carried out at a flat roller speed of 360 rpm. The thickness of the rice quaker made traditionally, 0.98 mm, can be approached by flattening using a machine at a gap width of 0.8 mm with 2 flakes resulting in a thickness of 0.96 mm quaker with a percentage of damage of 38.52%. In general, the level of damage to the resulting rice quaker is still very high, so further analysis is needed.Keywords: Rice quaker, gap width, flattening machine, flat rollers.
<p><em>The increasing number of vehicles every year provides opportunities to vehicles service. Vehicle components that often serviced or overhaul is the valve mechanism. How to remove the valve from the cylinder head generally use a manual valve remove tool. The time required to remove the valve using the tools need a long time. Effort to overcome these problems is to modify the existing valve remove mechanism. The purpose of this research is to design and test the performance of valve remove using lever mechanism. Performance test was conducted to determine the press force value to remove the valve, the percentage increase performance and time to remove the valve. The main components of the valve remove tool using the lever mechanism is frame, table, pole support, locking, hand grips, hydraulic, lever pusher and shaft sled. Testing using the valve mechanism is contained in the cylinder head Toyota Kijang 4K. The valve remove tool design has a simple form, easy to make, cheap, but has very good performance. The smallest of the press force to remove the valve is 129 N obtained at a distance of lock and poles support as far as 22 cm. The valve remove tool using the lever mechanism was design can remove the valve from the cylinder head in time 26,17 seconds/valve or 418,67 seconds to remove 16 valves on the cylinder head. This tool is able to improve the performance of manual valve remove tool screw type by 76,28%, and can improve the performance valve remove tool the pneumatic system by 65,79%.</em></p>
<p class="Default"><em>Coconut coir can be processed into cocopeat and coco fiber. In the chopping process, the chopping mechanism has a critical role that will determine the results of the chopping off of coconut coir. Based on these conditions, in this study, the development of a chopping mechanism was carried out by modifying the chopper blade to improve the chopper of coconut coir. The purpose of this study was to modify the coconut coir chopper blade, perform performance tests and calculate the increased performance after modification. Modification of the chopper mechanism on the coconut coir chopper machine is done by replacing the type of chopper blade with an iron rod with a diameter of 4 mm which is sharpened at the end. The test data includes data on the capacity of coconut coir chopping, the percentage of cocopeat, the percentage of coco fiber, the percentage of unprocessed coconut coir, the percentage of material loss, and the increase in performance after modification. The modified coconut coir chopper mechanism has specifications of 240 mm long, 100 mm diameter, 39 blades, and ± 14 mm high. The test was carried out at a rotary speed of the chopper mechanism of 720 rpm. Based on the test result, the capacity of chopping coconut coir using a modified coconut coir chopper machine is 7,93 kg/hour, producing 45,57% cocopeat, 36,15% coco fiber, 13,15% coconut coir unprocessed and the loss reached 5,13%. Modifications on the chopper blade are proven to increase the performance of the coconut coir chopper machine by 297%.</em></p>
scite is a Brooklyn-based organization that helps researchers better discover and understand research articles through Smart Citations–citations that display the context of the citation and describe whether the article provides supporting or contrasting evidence. scite is used by students and researchers from around the world and is funded in part by the National Science Foundation and the National Institute on Drug Abuse of the National Institutes of Health.
customersupport@researchsolutions.com
10624 S. Eastern Ave., Ste. A-614
Henderson, NV 89052, USA
This site is protected by reCAPTCHA and the Google Privacy Policy and Terms of Service apply.
Copyright © 2024 scite LLC. All rights reserved.
Made with 💙 for researchers
Part of the Research Solutions Family.