In shell side mode, PDMS was more efficient and no wetting phenomenon was 23 observed with this contactor. The differences have been explained, taking into account 24 2 the material properties (porosity, material resistance …) of the membrane and structure 25 (packing density, fibre diameter …) of the modules. Methane removal efficiencies of up 26 to 98% could be achieved, showing the viability of methane removal/recovery using this 27 technology. Simultaneous degassing of CO 2 was also monitored in both modules, 28 showing that the removal efficiency of this gas was considerably lower than for 29 methane. In general terms, the removal of dissolved CO 2 followed a quite similar 30 behaviour from that described for methane. Experimental overall mass transfer 31 coefficients were also obtained. 32
Keywords 33Anaerobic reactor; degassing; greenhouse gas emissions; membrane contactors; 34 methane recovery 35 36 3
Laboratory bench-scale experiments were conducted to investigate the performance of primary sludge fermentation for volatile fatty acids production. Primary sludges from two major wastewater treatment plants located in Valencia (Pinedo and Carraixet) were used. Experiments were performed at solids retention times between 4 and 10 days, and total volatile solids concentrations between 0.6% and 2.8%. Operation at two temperatures (20 degrees C and 30 degrees C) was also checked. Results indicated the importance of feed sludge characteristics on volatile fatty acids yields, being approximately double for the Carraixet wastewater treatment plant sludge than for the Pinedo plant. In both cases, higher volatile fatty acids yields were observed at higher total volatile solids concentrations. Solids retention times above 6 days scarcely improve volatile fatty acids yields, while experiments conducted at 4 days of solids retention times show an important decrease in volatile fatty acids yields. On raising temperature an increase in volatile fatty acids yields was observed, mainly due to an improvement in the hydrolysis of particulate organic matter.
A 0.75-m 3 pilot-scale biotrickling filter was run for over 1 yr in a Spanish furniture company to evaluate its performance in the removal of volatile organic compounds (VOCs) contained in the emission of two different paint spray booths. The first one was an open front booth used to manually paint furniture, and the second focus was an automatically operated closed booth operated to paint pieces of furniture. In both cases, the VOC emissions were very irregular, with rapid and extreme fluctuations. The pilot plant was operated at an empty bed residence time (EBRT) ranging from 10 to 40 sec, and good removal efficiencies of VOCs were usually obtained. When a buffering activated carbon prefilter was installed, the system performance was improved considerably, so a much better compliance with legal constraints was reached. After different shutdowns in the factory, the period to recover the previous performance of the biotrickling reactor was minimal. A weekend dehydration strategy was developed and implemented to control the pressure drop associated with excessive biomass accumulation.
Three laboratory-scale peat biofilters were operated at 90 s empty bed residence time (EBRT) for over a year. Biodegradation of ethyl acetate, toluene, or a 1:1 mixture were investigated. In first stage, inlet concentration was progressively increased from 0.4 to 4.5 g/m(3). The maximum elimination capacity (EC) found for ethyl acetate was 190 gC/m(3).h, and it was not affected by toluene. The maximum EC found for toluene as a sole contaminant was 150 gC/m(3).h, but the presence of ethyl acetate decreased the toluene maximum EC to 80 gC/m(3).h. From respirometry monitoring, values of 3.19 g CO(2)/gC and 3.06 g CO(2)/gC for pure ethyl acetate and pure toluene, respectively, were found, with overall yield coefficients of 0.13 g dry biomass produced per gram ethyl acetate consumed and 0.28 g dry biomass produced per gram toluene consumed. CO(2) production in the 1:1 mixture was successfully simulated. Dynamics of living and dead cells were monitored in four sections of the biofilters. Concentrations ranged between 2.6 x 10(9) and 3.0 x 10(10) cells per gram-dry peat for total bacteria, and 2.4 x 10(9)-1.9 x 10(10) cells per gram-dry peat for living bacteria. At high loads loss of bacterial density in the inlet zones, and increase in the dead cells percentages up to 60% was observed. In second stage, long-term performance at an inlet concentration of 1.5 g/m(3) was evaluated to show the process feasibility. Good agreement with previous data was obtained in terms of EC and CO(2) production. Restoration of living cells proportion was also observed.
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