Endovascular repair of the thoracic aorta has been adopted as the first-line therapy for much pathology. Initial results from the early-generation endografts have highlighted the potential of this technique. Newer-generation endografts have now been introduced into clinical practice and careful assessment of their performance should be mandatory. This study describes the initial experience with the Valiant endograft and makes comparisons with similar series documenting previous-generation endografts. Data were retrospectively collected on 180 patients treated with the Valiant endograft at seven European centers between March 2005 and October 2006. The patient cohort consisted of 66 patients with thoracic aneurysms, 22 with thoracoabdominal aneurysms, 19 with an acute aortic syndrome, 52 with aneurysmal degeneration of a chronic dissection, and 21 patients with traumatic aortic transection. The overall 30-day mortality for the series was 7.2%, with a stroke rate of 3.8% and a paraplegia rate of 3.3%. Subgroup analysis demonstrated that mortality differed significantly between different indications; thoracic aneurysms (6.1%), thoracoabdominal aneurysms (27.3%), acute aortic syndrome (10.5%), chronic dissections (1.9%), and acute transections (0%). Adjunctive surgical procedures were required in 63 patients, and 51% of patients had grafts deployed proximal to the left subclavian artery. Comparison with a series of earlier-generation grafts demonstrated a significant increase in complexity of procedure as assessed by graft implantation site, number of grafts and patient comorbidity. The data demonstrate acceptable results for a new-generation endograft in series of patients with diverse thoracic aortic pathology. Comparison of clinical outcomes between different endografts poses considerable challenges due to differing case complexity.
Objectives To investigate the concept of ‘urethral atrophy’, which is often cited as a cause of recurrent incontinence after initially successful implantation of an artificial urinary sphincter (AUS); and to investigate the specific cause of the malfunction of the AUS in these patients and address their management. Patients and Methods Between January 2006 and May 2013, 50 consecutive patients (mean age 54.3 years) with recurrent incontinence had their AUS explored for malfunction and replaced with a new device with components of exactly the same size, unless there was a particular reason to use something different. Average time to replacement of the device was 10.1 years. The mean follow‐up after replacement of the device was 24.7 months. All patients without an obvious cause for their recurrent incontinence had preoperative urodynamic evaluation, including measurement of the Valsalva leak point pressure (VLPP) and the retrograde cuff occlusion pressure (RCOP). After explantation of the AUS in patients without any apparent abnormality of the device at the time of replacement, the pressure generated by the explanted pressure‐regulating balloon (PRB) was measured manometrically, when this was possible. In a select group of six consecutive patients of this type, the fibrous capsule surrounding the old cuff was incised then excised to expose and evaluate the underlying corpus spongiosum. Results In 31 of the 50 patients (62%) undergoing exploration, a specific cause for the malfunction of their AUS was defined. In the other 19 patients (38%) no cause was found, either preoperatively or at the time of exploration, other than a low VLPP and RCOP. A typical ‘waisted’ or ‘hour‐glass’ appearance of the underlying corpus spongiosum was demonstrable, to some degree, on explanting the cuff in all cases. In the six patients in whom the restrictive sheath surrounding the cuff was excised, the urethral circumference immediately returned to normal after the compressive effect of the sheath was released. Manometry of the explanted PRBs, when this was possible, showed a loss of pressure in all instances. Replacement of the explanted AUS with a new device with the same size cuff and PRB in 14 of these 19 patients was successful in 12 (85.7%). Conclusions These results, and other theoretical considerations, suggest that recurrent incontinence, years after initially successful implantation of an AUS, is because of material failure of the PRB, probably attributable to its age and consequent loss of its ability to generate the pressure it was designed to produce, and that urethral atrophy does not occur. Simply replacing the old device with a new one with the same characteristics, unless there is a particular reason to do otherwise, is usually successful and avoids the complications of alternatives such as as cuff downsizing, implanting a PRB with a higher pressure range, implantation of a second cuff or transcorporeal cuff placement, all of which have been advocated in these patients.
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