The degradation of alloy 600 and its weld material (alloy 82/182) has been reported in many nuclear power plants. In Korea, the crack induced by PWSCC was discovered in the drain nozzle of Yongkwang units 3 & 4 in 2006∼2008 and SG plug weld of Yongkwang unit 3 in 2007. In July 2007, during visual inspections of SG tube plugs at Yonggwang unit 4, boric acid deposits were observed around five Alloy 600 welded plugs. The root cause of the cracking in alloy 600 plugs was revealed to be due to the fact that the cracks were mainly caused by residual stress induced from the welding, expanding and tight-fitting. Younggwang unit 3 found the white small deposits on the drain nozzle on the 10th RFO in 2007. The root cause of the cracking in drain nozzle was revealed to be due to the initiation of a crack on the inside surface of drain nozzle and propagated to through wall cracks in the axial and circumferential direction. Younggwang unit 3 found the white widespread deposits on the upper head of a reactor vessel on the 12th RFO in 2010. Utility is trying to reveal the root cause of the cracking in the vent line of the reactor head according the KINS requirement. In this article, Korean regulatory experiences for PWSCC are introduced. After these PWSCC experiences, all SG tubes welded by Alloy 600 were replaced and all SG drain and instrumentation nozzles with Alloy 600 have been replaced into Alloy 690 material.
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