In this study, a 4UM-120D electric leafy vegetable harvester was employed as the research object. An automatic control system was created to maintain the cutter’s height above the ground within ±2% of the desired value. The intention was to reduce the operators’ work intensity while improving the leafy vegetable harvester’s working quality. The automatic control system for the cutter height from the ground was explained, along with its structure and operating philosophy. MATLAB was used to establish the two-phase hybrid stepper motor’s mathematical electrical equation and mechanical equation models. An analysis was carried out on the fundamentals and differences between position PID and incremental PID control algorithms. Utilizing incremental PID in combination, the control strategy for the harvester cutter height from the ground was built, and an automatic control system was produced under the corresponding control strategy. The stability, accuracy, and rapidity of the automatic control system of the cutter height from the ground under the incremental PID control strategy were analyzed by simulating different actual working conditions with MATLAB/Simulink and taking the steady-state transition time as the evaluation index. The test results show that when the deviation between the current value and the set value was greater than 2%—that is, when the harvester was in the condition of suddenly crossing the ditch or suddenly climbing the slope—the automatic control system based on the incremental PID control strategy had a good dynamic response performance and stability. This resulted in the automatic control function of the harvester cutter height off the ground being achieved. When the rotation angle PID control algorithm’s proportional coefficient is Kp = 4.665, the rotation speed PID control algorithm’s proportional coefficient is Kp = 5.65 and its integral coefficient is Ki = 3.86, and the current PID control algorithm’s proportional coefficient is Kp = 0.5455 and its integral coefficient is Ki = 30.4578. The harvester abruptly crossed a ditch while operating steadily, and the automatic control system’s steady-state transition time for the height of the cutter off the ground was 1.0811 s. The harvester abruptly climbed a slope while operating steadily, and the automatic control system’s steady-state transition time for the height of the cutter off the ground was 1.1185 s. Data from the field tests revealed a degree of reliability in the simulation test results. The study offered a strategy for raising the harvester quality for leafy vegetables while lowering the operator workload.
This paper used the 4UM-120D electric leafy vegetable harvester as the research object and designed a travel speed automatic control system to maintain the travel speed within a set value of ±2% in order to improve the efficiency and quality of leafy vegetable harvester operations and decrease the work intensity of the operator. The harvester’s travel speed was automatically controlled by using the PID, adaptive fuzzy PID, and sliding mode control techniques after the mechanical and electrical equations for the travel drive motor (a DC brushless motor) were established in MATLAB. By simulating various working situations, the stability, accuracy, and speed of the automatic control system were compared and analyzed using the adjustment time, overshoot, steady-state transition time, and maximum deviation from the set speed as evaluation indicators. The test results revealed that when the current value of the leafy vegetable harvester travel speed deviated from the set value by more than 2%, the dynamic response performance and stability of the DC brushless motor travel drive system based on the sliding mode control strategy was significantly better than that of the PID and adaptive fuzzy PID control strategies, and its anti-disturbance was stronger, achieving the function of automatic control of the harvester travel speed. When the travel motor started with a constant load and the sliding mode control strategy’s parameters were the gain factors A = 1/70, c = 100, ε = 100, and k = 100, the travel drive system regulation time was 1.5 s, and the overshoot was 10%. When the harvester was operating smoothly and had leafy vegetable collection baskets loaded and unloaded, the steady-state transition time was 0.3 s. According to the actual engineering application experience, the specific technical state of the control strategy of the agricultural machinery travel speed automatic control system was: regulation time 2.5~3 s; overshoot amount 20~25%; and steady-state transition time 1.0~1.5 s, so the travel speed automatic control system of the electric leafy vegetable harvester in sliding mode was in line with the technical state requirements. The results of the field trials demonstrated the accuracy of the simulation test results. This study offered a method to lessen the work intensity of operators and increase the operating efficiency and quality of a leafy vegetable harvester.
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