This paper is to explain the optimization of using Modified Shale Inhibitor Water Based Mud (WBM) to drill up to 5,500 ft interval of K-formation reactive shale on South-S Gas Wells.
By combining a comprehensive method consists of drilling fluid laboratory test and lessons learned in S area, the optimization was done by determining the amount or concentration of Polyamine & KCl combination, pure Polyamine, Polyamine & NaCl combination, and Pure KCl-Polymer in WBM system as a shale inhibitor. The comparison of shale inhibitor compositions were made by comparing the achieved optimization of drilling fluid program such as drilling time, cost economic, and environment aspect.
The basic idea of the WBM optimization was to improve drilling time during drill 5,000 ft footage in 12-1/4" hole section in reactive shale formation as per drilling program. Laboratory test consists of Linear swelling meter with various parameter concentration of Polyamine & KCl combination, pure Polyamine, Polyamine & NACl combination, and Pure KCl-Polymer in WBM system as a shale inhibitor and cation exchange capacity test (CEC or MBT) was done using composite of offset well shale cutting. Experience showed that on 12-1/4" hole section, while facing reactive shale (CEC 18 - 24 meq/100 gr) from K-formation on South-S, modified WBM was proven to eliminate reactive shale issues and lead to budget saving without environmental issues.
For S-15 and S-14 wells at South S Field, drilling of the 12-1/4” hole section became the longest tangent hole section interval of both wells. There were several challenges identified where hole problems can occur. The hole problems often occur in the unconsolidated sand layers and porous limestone formation sections of the hole during tripping in/out operations. Most of the hole problems are closely related to the design of the Bottom Hole Assembly (BHA). In many instances, hole problems resulted in significant additional drilling time. As an effort to resolve this issue, a new BHA setup was then designed to enhance the BHA drilling performance and eventually eliminate hole problems while drilling. The basic idea of the enhanced BHA is to provide more annulus clearance and limber BHA. The purpose is to reduce the Equivalent Circulating Density (ECD,) less contact area with formation, and reduce packoff risk while drilling through an unconsolidated section of the rocks. Engineering simulations were conducted to ensure that the enhanced BHA were able to deliver a good drilling performance. As a results, improved drilling performance can be seen on S-14 well which applied the enhanced BHA design. The enhanced BHA was able to drill the 12-1/4” tangent hole section to total depth (TD) with certain drilling parameter. Hole problems were no longer an issue during tripping out/in operation. This improvement led to significant rig time and cost savings of intermediate hole section drilling compared to S-15 well. The new enhanced BHA design has become one of the company’s benchmarks for drilling directional wells in South S Field.
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