Executive SummaryWashington River Protection Solutions requested that at least 4 L of Hanford tank waste collected from tank 241-AP-105 and diluted to approximately 5.6 M Na (AP-105DF) be prepared for use in vitrification studies. Cesium removal was required to meet this objective and the waste pretreatment platform, established at Pacific Northwest National Laboratory, was used to create the vitrification feed. The Test Platform mimicked the Low-Activity Waste Pretreatment System (LAWPS) facility planned to pretreat Hanford tank waste supernate by removing solids in a cross flow filter apparatus and processing the supernate through ion exchange columns to remove cesium. At the time of testing, the ion exchange media was targeted to be spherical resorcinol-formaldehyde (SRF) resin. 1 The SRF resin has been tested with a wide array of simulants and process scales, but column performance testing with actual tank waste had been somewhat limited to two Hanford tank wastes (AP-101 and AN-102) in up to two process cycles. This report describes testing conducted in a total of six load elute cycles with the AP-105DF tank waste. The column system was first tested with simulant and was previously described 2,3 ; this report describes the six process cycle results with the AP-105DF tank waste.Column testing was conducted on SRF resin provided by Microbeads AS (Skedsmokorset, Norway, batch number 1F-370/1392), which was manufactured in August 2011. The column testing was prototypic to the intended LAWPS operations in a lead-lag column format, albeit on a small-scale basis with 10-mL resin beds. In this configuration, neither the length-to-diameter ratio nor the superficial flow velocity matched the full-scale design. In this process, the feed was directed downflow through the lead column and then through the lag column. Loading continued until the lag column reached 10% of the Hanford Tank Waste Treatment and Immobilization Plant contract limit for receiving supernatant waste for vitrification (a function of the Na and 137 Cs concentrations). As a result of this process condition, the lead column was nearly saturated with Cs. After loading, the feed was displaced with 0.1 M NaOH, and then the columns were rinsed with water in a downflow lead-to-lag configuration. Elution was conducted downflow from the lag to the lead column with 0.45 M HNO 3 followed by a water rinse. The resin was returned to the Na-form by processing 1 M NaOH downflow from the lag to the lead column, which deviated from the intended LAWPS process operation where the regeneration would occur in upflow to fluidize the resin beds. Variations to the feed flowrates, elution volumes, and elution flowrates were implemented to evaluate effects on the Cs load behavior and Cs leakage to the next process cycle.Cs load and elution profiles were generated. From the load profile, the number of bed volumes (BVs) processed to reach 50% breakthrough on the lead column was determined along with the number of BVs processed before reaching 10% of the contract limit on the l...