2016
DOI: 10.1177/0954410016673093
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Experimental investigation on flow unsteadiness during spike stall suppression process in an axial compressor via air injection

Abstract: Stall recovery process for performance enhancement of an axial compressor has been experimentally carried out using air injection at its rotor blade row tip region. Twelve air injectors had been mounted evenly spaced around the compressor casing upstream the rotor blade row. Instantaneous flow velocities at various radial and circumferential positions were measured simultaneously utilizing hot wire anemometry. These unsteady results, separately presented in frequency and time domains, provided to distinguish s… Show more

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Cited by 4 publications
(4 citation statements)
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“…It can be deduced from this figure that the maximum difference between the present numerical results with each of the experimental results is about 12%, which seems appropriate.
Figure 7 Comparison of performance curves between present results and available experimental data 8 , 10 .
…”
Section: Numerical Simulation Procedures and Boundary Conditionsmentioning
confidence: 91%
See 2 more Smart Citations
“…It can be deduced from this figure that the maximum difference between the present numerical results with each of the experimental results is about 12%, which seems appropriate.
Figure 7 Comparison of performance curves between present results and available experimental data 8 , 10 .
…”
Section: Numerical Simulation Procedures and Boundary Conditionsmentioning
confidence: 91%
“…To validate the numerical results, performance curve of the plane case (i.e., no treatment) in terms of the total pressure rise coefficient versus the flow coefficient are compared with those of Inoue et al 10 and Taghavi et al 8 which are carried out experimentally. These results are shown in Fig.…”
Section: Numerical Simulation Procedures and Boundary Conditionsmentioning
confidence: 99%
See 1 more Smart Citation
“…This rotor has already been tested experimentally by Inoue 28 . www.nature.com/scientificreports/ Taghavi et al 29 have already conducted many tests on this rotor blades row in a low speed axial compressor test-rig located at the Aerodynamic and Compressible Turbomachine Research Laboratory of the Iran University of Science and Technology (IUST-ACTLab). The layout of this test-rig is shown in Fig.…”
Section: Model Specificationsmentioning
confidence: 99%