Volume 2A: Turbomachinery 2018
DOI: 10.1115/gt2018-76826
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Numerical and Experimental Investigations on Optimized 3D Compressor Airfoils

Abstract: The objective of the presented work is to perform numerical and experimental studies on compressor stators. This paper presents the modification of a baseline stator design using numerical optimization resulting in a new 3D stator. The Rolls Royce in-house compressible flow solver HYDRA was employed to predict the 3D flow, solving the steady RANS equations with the Spalart-Allmaras turbulence model, and its corresponding discrete adjoint solver. The performance gradients with respect to the input design parame… Show more

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Cited by 8 publications
(9 citation statements)
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References 27 publications
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“…objectives, [34] decreased the exit flow angle by 38.6% and the total pressure losses by 3.2% w.r.t. the baseline.…”
Section: Tub Compressor Stator Optimizationmentioning
confidence: 96%
See 1 more Smart Citation
“…objectives, [34] decreased the exit flow angle by 38.6% and the total pressure losses by 3.2% w.r.t. the baseline.…”
Section: Tub Compressor Stator Optimizationmentioning
confidence: 96%
“…The TurboLab Berlin compressor stator common research model has been tested in the measurement rig of the Chair for Aero Engines at TU Berlin. In the past, several research groups from academia and industry studied this case [31][32][33] and experiments were conducted on the original geometry and one optimized by Rolls-Royce Deutschland [34]. This stator is an aerodynamic model of a blade typically found in modern jet engine compressors.…”
Section: Tub Compressor Stator Optimizationmentioning
confidence: 99%
“…In order to validate the improved performance of the OPS, measurements were carried out for all three operating conditions using the experimental setup/procedure presented in subsection 2.7.2. whereas its performance at OD+ seems to be slightly worse (increased loss values for most of the passage height). More details regarding this comparison can be found in [209]. To conclude this subsection, the superior performance of the OPS geometry ob-…”
Section: Experimental Validation Of Resultsmentioning
confidence: 96%
“…All the experiments were carried out using a low-speed open circuit wind tunnel at the Chair for Aero Engines of TUB [209], depicted in the schematic of fig. The annular measurement rig consists of the highly loaded compressor stator cascade.…”
Section: Experimental Setup/proceduresmentioning
confidence: 99%
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