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Cement packer well work is a rig-less intervention method for accessing reserves above and between production packers. It is used to isolate a target completion interval from other hydrocarbon or non-hydrocarbon zones. Cement packer is used as an alternative to the conventional production packer. The key benefit of cement packer application is the cost savings (in the order of $MM) realized instead of using a major rig workover to achieve the same objective of isolation of a target interval. A key challenge however is the attendant increased skin caused by reduced perforation efficiency through the extra layer of cement plug. This paper addresses this issue by showing the work-around adopted by one of the Assets in Chevron Nigeria JV to improve well productivity. Well-AA was evaluated and proposed for a zone switch non-rig workover intervention of the production interval from N-AA/Well-AA to K-AA/Well-5X reservoir in November 2012 using cement packer to isolate existing completion and recomplete in the new target reservoir. The zone switch and perforation were executed successfully via a cement packer operation but didn't flow after perforation. Several attempts to bring the well on production such as swabbing were made with no success. The outcome of the attempts indicated there was poor or lack of connectivity between the wellbore and the sand-face. A well performance lookback was done to identify the well problem and it was recommended to re-perforate the proposed interval of the well and initiate gas lift. The recommendation for re-perforation was based on productivity index analysis of previous cement packer completions and the perforation gun performance with respect to the required penetration through the cement plug, tubing/casing and the formation. Estimated productivity index (PI) from two previous cement packer operations were the basis of the recommendation. Well-BD (was perforated twice) with calculated PI of 2 Bbls/Day/Psi and Well-CX (which was perforated once) with calculated PI of 0.3 Bbls/Day/Psi. This paper will discuss the lessons learnt and best practice from re-perforation of Well-AA with a bigger and deeper penetrating perforation gun that restored initial production from 0 BOPD to 550 BOPD at natural flow condition via a SEWOP barge operation.
Cement packer well work is a rig-less intervention method for accessing reserves above and between production packers. It is used to isolate a target completion interval from other hydrocarbon or non-hydrocarbon zones. Cement packer is used as an alternative to the conventional production packer. The key benefit of cement packer application is the cost savings (in the order of $MM) realized instead of using a major rig workover to achieve the same objective of isolation of a target interval. A key challenge however is the attendant increased skin caused by reduced perforation efficiency through the extra layer of cement plug. This paper addresses this issue by showing the work-around adopted by one of the Assets in Chevron Nigeria JV to improve well productivity. Well-AA was evaluated and proposed for a zone switch non-rig workover intervention of the production interval from N-AA/Well-AA to K-AA/Well-5X reservoir in November 2012 using cement packer to isolate existing completion and recomplete in the new target reservoir. The zone switch and perforation were executed successfully via a cement packer operation but didn't flow after perforation. Several attempts to bring the well on production such as swabbing were made with no success. The outcome of the attempts indicated there was poor or lack of connectivity between the wellbore and the sand-face. A well performance lookback was done to identify the well problem and it was recommended to re-perforate the proposed interval of the well and initiate gas lift. The recommendation for re-perforation was based on productivity index analysis of previous cement packer completions and the perforation gun performance with respect to the required penetration through the cement plug, tubing/casing and the formation. Estimated productivity index (PI) from two previous cement packer operations were the basis of the recommendation. Well-BD (was perforated twice) with calculated PI of 2 Bbls/Day/Psi and Well-CX (which was perforated once) with calculated PI of 0.3 Bbls/Day/Psi. This paper will discuss the lessons learnt and best practice from re-perforation of Well-AA with a bigger and deeper penetrating perforation gun that restored initial production from 0 BOPD to 550 BOPD at natural flow condition via a SEWOP barge operation.
The Cement Packer completion has found great use and applicability in Chevron Nigeria assets by creating a cost-effective way of accessing ‘behind-pipe’ production opportunities. These isolated hydrocarbon pools could not have been otherwise developed due to the un-favourable cost of a Major Rig Workover. This has helped to maximize value from oil and gas assets by returning previously inactive wellbores to production. The typical through-tubing technique of deploying cement packers in candidate wells has been to set a plug in the tubing to isolate the deeper reservoir, punch a hole in the tubing, displace cement through the hole in the tubing and place it across the new target sand so that the displaced cement would serve as an artificial packer in the tubing-casing annulus. The tubing would then be perforated across the cement packer and into the target reservoir. Much success has been recorded with the use of this technique and though it has provided proper tubing-casing annulus isolation, there have also been a few challenges. Some of the challenges include significant skin (caused by the extra pressure drop during fluid flow through the cement tunnel), limited perforation efficiency in dual-string wells (caused by gun-size limitations due to the tubing size) and lack of radial flow since the perforations are oriented at zero-degree phasing to avoid perforating into the second string in dual-string wells. Eliminating these challenges would significantly improve the well production rate and project economics. This paper presents three case studies where these challenges have been effectively addressed and the attendant results. In the first case study, we show how over-displacing the cement ensured that the column of cement was placed above (rather than across) the proposed completion perforations while still retaining annular isolation. This significantly improved the expected initial production rate of the well by a factor of more than three since there was no extra skin due to fluid flow through the cement tunnel. In the second case study, we show how we improved the perforation efficiency in a dual-string well despite being constrained by the gun size by perforating twice at zero-degree phasing. In the third case study, we show how we overcame the challenge of always perforating at zero-degree phasing in dual-string wells by performing dummy simulations (at the surface) using pipe-in-pipe configurations to better understand the perforating gun orientation downhole relative to the tubings and casing. Based on the results of the surface simulations, we achieved additional phasing in two perforation runs and this significantly increased the productivity of the well. A major lesson learnt was the importance of performing dummy simulations at the surface using pipe-in-pipe configurations to mimic the tubings-casing configuration. This was crucial to the success of the job where additional phased perforations were added.
The use of cement packers to access behind-pipe hydrocarbon opportunities has opened up significant reserves without the attendant cost of a rig. A key challenge with this technique is the attendant high skin that results from the cement packer which significantly impacts initial production rates and recoverable reserves. The objective of this paper is to share technique and lessons from a case study in a mature field, offshore Niger Delta where an innovative technique was employed to place the cement packer above the perforation interval in the target reservoir. This eliminated the skin due to the cement packer, leading to significantly higher initial production rates when compared to analog workovers. The paper details operational procedure during execution. The lack of a local precedent in the deployment of this type of cement packer presented a key challenge. Perforating the target reservoir and string without impacting the second string in the wellbore was another challenge. The initial production rate from the case study was 2200 BOPD vs 800 BOPD or less from analog cement packer workovers. A key lesson learned is that this solution is best suited to wellbores with a single production string only or multiple strings wellbores in which there is no further production utility for the additional strings. The follow on best practice from this lesson is to fully evaluate the wellbore utility for any identified opportunity of this sort to ensure the deployment of this method does not impede the utility of the wellbore for future reservoir management operations.
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